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Neptune MCB
#1
Guest_Roger_*
Posted 09 April 2005 - 12:02 PM
What's the chance of repairing one of these?
Anyone got a good one in their truck they can read a R-value for me?
Any reliable rebuilders out there?
#2
Posted 09 April 2005 - 06:07 PM
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#3
Guest_Roger_*
Posted 10 April 2005 - 11:57 AM
I'm going to try that fix mentioned at the link you provided. All I have to loose is about $30 and a small peice of my pride if I have to cut an additional $250 check for a new MCB.
However, as replacing the Door Lock Wax Motor is required, I'd like to retrofit my MAH3000AWW to the new Solenoid Door Lock mechanism.
Do you know if that's possible, either officially or otherwise?
I will report back everything I've discovered at the end of this quest.
#4
Guest_Roger_*
Posted 11 April 2005 - 05:50 PM
If your Neptune Washer doesn't Spin in the Spin Cycle and the "Door Locked" indicator light is not illuminated, then you have a Shorted (perhaps intermittently) Door Latch Wax Motor and a blown Master Control Board (probably R11).
The Components on the MCB directly effected are R11 and Q6. Others mentioned as potentials are R43 and Q2.
First, install the new Wax Motor Kit, Maytag #12002535 ($17 retail).
Second, remove and replace the Components called out in this photo (about $2 retail).
R11 a 3.9K Ohm Carbon or Carbon Film Resistor
Q6 a Triac NTE5656
R43 a 18K Ohm Carbon or Carbon Film Resistor
Q2 a Transistor NTE288
Some of these may not have failed, but for a total parts bill of under $2, replace them all and consider it a belt-and-suspenders solution.
Lastly, if you're suspicious of an identical future failure you can cut and install an in-line Fuse on the Brown Wire (Plug 7, Pin 4), (Holder Kit and pack of 500mA Fast Blow Fuses, about $5). Consider this the belt-and-suspenders and stay home solution.
Note: this Board is not built to withstand all but the slightest heat soaking so the Solder Leads were trashed at R11 and required some creative scraping and soldering. And jumpers for good measure.
Samurai, if you email me your email I can forward a photo of the toasted MCB "with the lines and arrows and captions".
Roger
#5
Posted 12 April 2005 - 04:23 PM
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#6
Posted 18 April 2005 - 04:02 PM
Attached Files
#7
Posted 26 April 2005 - 06:17 PM
http://members.shaw.ca/gavb/
(Edit: which Samurai mentioned above :bathead: )
#8
Posted 11 May 2005 - 05:42 AM
#9
Posted 11 May 2005 - 07:05 AM
Only if you open the door!:poison:Are these Neptune still smelly?
#10
Guest_hason3_*
Posted 11 October 2005 - 04:50 PM
#11
Posted 11 October 2005 - 06:26 PM
From this great historical lesson, I infer that you must locate the source of the smoking: the motor? the machine control board? that rancid Pakistani's bowels? Let us think on these things.
Allahu Akbar!
#12
Posted 12 October 2005 - 01:47 AM
i replaced r11 and its still smoking
So, is that all you replaced r11?
If so, then that is your problem. You did not correct the problem that originally burned out r11.
You must read all the info and the links, (words in blue), in this discussion to correctly do this repair.
If r11 is burned the orginal problem that caused this part to fail has to be replaced first, (that would be the door latch "wax motor"). Also you must replace the q6 triac that controls the wax motor door lock circuit.
Willie's Budget Appliance Repair
Eureka, CA 95501
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